Author: admin

  • 17/03/19 -“You only paint them”

    17/03/19 -“You only paint them”

    We have heard in the past that some say we only repaint our vehicles,  I hope those that once thought that have had a change of opinion and that the last 3 weekends reinforce that opinion.  Work of cause continues on M500954.  First job to complete the East side.  Door planks were trimmed and any areas that will allow moisture in were sealed.

     

    On to the west side which traditionally is the weathered side and this one is no exception. We focused on the North corner and as the bolts were removed the side basically fell out.

     

    Jake then cleaned down and applied red oxide to the back of the frame whilst I manufactured a plate to cover the hole that has allowed water into and subsequently rot the van side.

     

    With the wind whipping around the now open side the red oxide dried very quickly.  The planking then began.  Once we got half way up recesses were cut to allow the planks to sit flush despite four rivets.

     

    Once fully planked plywood inner sheets were cut to size, fitted, holes drilled and bolts fitted, with the final task for Saturday to screw areas on the inner ply skin that was not supported by bolts.

     

    As can be seen, quite a transformation if we don’t say so ourselves.Untitled-1
    On to Sunday and attention turned to the West side door.  The old planks were removed, well fell off if we are once again being honest. As well as the locking catch.

     

    Some of the rot had penetrated into the inner planks so these were also removed as required.  This allowed access for Jake to clean and red oxide the doors centre bar.20190317_095652.jpg

    The plan is not to remove this door but a few areas were tight, so the remaining planks were sanded down to allow clearances to allow the door to slide easily. Measurements were taken and a suitable piece of ply was cut to size and fitted.

     

    Jake primed the edges before fitment and then the outer face once in position, the new door planks were also trimmed to size and locking catch refitted.

     

    The planks were of cause fitted, bolted and screwed top and bottom.

     

    Last job was to clean and hoover the inside ready for the final push.20190317_154646

    This completes this weekends work, we are 5/6th of the way through with just one corner to go.  This of cause will be the topic for next weekends update.20190317_155605

     

     

  • 03/03/19 – Business as usual

    As the title suggests we have returned to what we can only describe as our usual business. M500954, the LMS boxvan, is our next project.  The first task was to measure the vehicle so accurate replacement planks can be ordered.

     

    With measurements taken attention turned to the east side of the vehicle.  The door was removed, this basically fell off as it was quite rotten. My job being to dismantle it, salvage the steel fittings and as much wood as possible.

     

    Although the frame remains most of this will require replacement but it is being retained for templating.  Nick, Ross and Jake removed the bolts from the side planks and dismantled the inner and outer skins.

     

    All of the metal components removed from the door and an L angle from the frame were scraped down, cleaned up and red oxide applied.

     

    The last job for Saturday was to red oxide the frame were the L angle mentioned above lives.  This angle tightens the gap between frame and door when it is closed, a metallic draft excluder if you will.  Straight on to Sunday and with both frame and L angle dried they were bolted back together.

     

    Sunday morning was spent at Loughborough.  With preparations for unifying the GCR with its Northern counterpart, a number of grounded vans are requiring to be removed.  We have earmarked a number for possible future use but our trip was to collect spares that could be more useful in the short term. We have also looked at the viability of the Containers so expect further news on these.

     

    Back to Quorn and we were happy to have a further visit from Dave Bower.  We have some exciting ideas for Test Car 2 which we will shed light on in future updates.

    Jake returned to work on M500954 and applied red oxide to the back of all of the now exposed metal work.  Ross took a look at the Slip Working headlight whilst I looked at the possibility of manufacturing chalkboard brackets.  I am happy with the result.

     

    This week we shall be placing orders for wood and hopefully delivery will be in time for next weekends activities, we, as always shall keep you up to date.

  • 17/02/19 – A Buckeye? That’s not a wagon coupling, how does that go on……

    This week on Tuesday and Wednesday a number of our vehicles were used during a Timeline Events charter.  As usual, I was on site reenacting with Jack, but this time we were also joined by Ross.  If you have ever wondered what happens to van sides that have been removed? We repurpose them and this week the VEA door skins removed in 2017 became a headboard for Standard 5 73156.  The original was carried by the engine in 1959.

    On to the weekend and our vacuum adventures with Test Car 2 continue,  with the performance of the 15″ cylinder below par the decision was taken last weekend to replace it.  With the vehicle being made available for possible future use in passenger rakes the reduced braking provided by the reduced size cylinder could be detrimental to the braking of a train.  First, we dropped into Quorn to pick up one of our spare 21″ cylinders.  This was refurbished some time ago but not fully assembled whilst it awaited a purpose.  It originally came from one of our Dogfish hoppers and had been attacked by the tin worm.  The Cylinder dome was repaired by the locomotive department some years ago.20190216_092253

    On arrival at Rothley the first task was to remove the 15″ cylinder.

    With the cylinder removed, we had to modify a support bracket for the ETH through wire as this will be foul of a 21″ cylinder.  The clamp blocks were fully removed, the outer block was reduced to top and bottom radiuses and the inner block was cut down and the lower corner removed.

    Whilst Ross and I removed the 15, Nick and Jake assembled the 21. This included applying red oxide to the areas that will be out of reach when the cylinder is fitted.  The inside was hovered, a new seal fitted and cylinder bolted up.  The repairs previously carried out are clearly visible.

    With the cylinder assembled, it was time to fit it to the vehicle.  The trunion supports were replaced with standard brackets recovered from long lost coaches and the cylinder lifted into position.  The cylinder was connected to the brake cross shaft, release valve fitted and clearances checked.

    Once complete Jake took the time to red oxide the rest of the cylinder but not before the all-important vacuum test.  20inHg was reached and the cylinder operated a number of times before the vacuum was destroyed.  10 minutes came and past and the brake was still applied after 3 hours and deemed a success.20190216_163138

    Next task was to replace the draw hook at the generator end.  When converted to a test car in 1974 the original draw hook with buckeye attachment was removed and replaced with that from a 20T Brake van.  This included a narrowing of the headstock slot which luckily was only a plate bolted into the original.

    Taken from another long since lost vehicle a full set of coach drawhook springs drawbar and draw-hook was retrieved from storage. Ross had the arduous task of undoing the mounting nut 1/8th of a turn at a time.  Once free the assembly was removed along with the headstock plate.

    A ware plate was fitted, the spring pack then assembled and fitted and the recovered draw bar and hook was also fitted,  All four members of the team were required with some interesting contortions of people around the axles, bogie and pipework of the coach.

    On to Sunday and again a quick visit to Quorn. This time to pick up a buckeye.  On arrival at Rothley the split pin to secure the draw hook was fitted.  Unfortunately, airlines were in the way but a quick modification to the support brackets and clearance was attained.

    Next job was the laborious task of screwing up the drawbar nut because of the bogie this was done 1/4 turn at a time.  Once tight the split pin was fitted.

    With the draw hook assembly complete next was the “simple” task of hanging the buckeye.  This required a few burs dressing and once in place, the support pin was driven home and once again a split pin fitted.

    When we dropped the buckeye however some minor alterations had to be carried out.  The buckeye came into contact with the main reservoir cock.  This was removed and then the support plate was foul.  A little alteration and the cock and support plate were clear.

    Back in the service position the release chain and support pin chain were fitted and the release tested.  A little lubrication and the wear limit was checked and the buckeye passed fit for use.

    The last item was to replace the internal arrangement drawing which I had created in the week and marks the start of the internal tidy and the task of replacing the faded signage. The new one may give a clue to the livery we are looking at applying.20190216_102639

    Hopefully, we will be back to normal next weekend or at least we will be back at Quorn.

     

     

     

  • 3/2/19 – Testing times ahead

    3/2/19 – Testing times ahead

    Before we move on to this weeks update, I was sent some images from James Brace who visited the railway during last weekends gala, he caught Nick, Ross and I conducting our duties as TPO Groundcrew.  Thank you James.

    This weekend we move on toa new arrival to the fleet.  Although it has been on the GCR for some time it has recently passed into our care.  ADB975397 or more commonly known as Test Car 2.  It gives me great pleasure to once again be responsible for this vehicle, it was myself that saved it from scrap in 2016 when it fell out of use on the Old Dalby Test Track.  In its glory days, it was used for the slip brake testing of rolling stock and latterly it was used for taking visitors up & down the test track.


    So this weekend our adventures take us to Rothley Carriage & Wagon.  We are preparing the vehicle before it is moved to Quorn as it will be our temporary base of operation whilst “the yellow coach” comes to Rothley for much-needed bodywork to be carried out.

    The vehicle has already had some work done by C&W staff.  The sealing of leaking windows and the refitment of Pullman gangway and matching buffers to the Generator end.  This is to enable the coach to be coupled with other coaches and increase the usability of the vehicle, most notably as an emergency brake vehicle if the need arises.

    On to this weekend and a wash and brush up to start the proceedings.  Jake took care of the interior with a hover and a wash of all surfaces,  I focused on the outside most notably the windows.

    In what can only be described as “playing”, me managed to get the lights throughout the vehicle working. Including the head and tail lamps.

    The headlight had an infestation of flies.  So this was removed for cleaning. Thankfully however the vehicle had a spare and more on that lower down this update.20190202_171223

    Between the slip end and the main saloon, there was a hole which was the location of test equipment long since removed.  This hole was filled and will help retain heat within the main saloon.

    The vehicle is laid out as follows:
    The South end has observation windows and was were the slip operation was controlled from.20190202_173213

    Next is the main saloon which held the monitoring equipment and instrumentation for recording the testing.  This would have been a hive of activity during testing.

    A small area for coats and baggage and a toilet are next.

    This is followed by a kitchen area and the Guards compartment.

    Then we have a workshop area and the main generator set. The workshop I spent Sunday tidying up.

    Looking in cupboards and behind panels, we found two noteworthy items.  A BR(M) Blanket and the original running number chalked on the back of an access panel.

    So on to Sunday and as mentioned above more time cleaning and tidying the Workshop area, before that however, I completed the installation of the replacement headlight, complete with double arrow.  The removed one will be stripped down and cleaned up and retained as a spare.

    During the tidy, the side panel for the equipment rack in the main saloon was found and duly refitted

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    Jake continued with a number of odd jobs.  Fitting the slip end microphones and refitting panels and trims that had been displaced.

    Before the vehicle left Old Dalby in 2016 I removed the owner’s plate that was located on the Kitchen Door.  This plate has been on my stairs at home for almost 3 years doing nothing but gathering dust.  I saw fit to return it to its original location after a quick polish.

    Ross fitted locks to the doors so we can secure the vehicle for our use

    20190203_125131

    The final task for the whole weekend was to reinstate the vacuum hoses, again found in the tidy up.  Having looked under the vehicle we knew at this stage it would only be a through-pipe but the main reason for refitting the hoses was to check its integrity. With Rothley’s vacuum test rig wound up the gauges dotted around the vehicle began to raise.  As can be seen in the images below 20 inHg was attained, this was seen on all gauges. A duplex in the slip end, one in the main saloon and the Guards gauge which was installed moments before the test.

    With the integrity of the through pipe confirmed next step is to reinstate the vacuum cylinders and hopefully we will have an operational vacuum brake.  But more on that next weekend.

     

     

  • 20/01/19. Shochood B, Aesthetically

    Another weekend and January is rapidly passing.  Work continues on the Shochood B and this should be the last update with a hoodless vehicle.  In preparation for the hood fitment, the missing loops for attaching said hood have been fitted.  These were manufactured by Jamie and Pat from Rothley C&W and our thanks go to them for helping with this project.
    As we do not have the capacity to weld, the side hoop was manufactured from threaded bar this allowed it to be bolted in position.  The end hoop was fitted to a mounting plate which was again bolted in position.

    Once these were fitted Nick and Jake turned to the ends.  Due to two large holes being drilled in each end this has allowed years of rust to accumulate.  This was removed and plates manufactured to fill the voids.  Again due to our welding inability theses plates were bolted in position and once better weather arrives will be filled.  Until then they have been redoxided along with the hoops fitted.

    My task and completing my personal mission to aesthetically create a Shoochood B, the end steps were both removed.

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    Saturday’s final task was to place the Palbricks toolbox back on the vehicle just to keep it out of the way until the vehicle’s future is fully decided.20190119_161913

    On to Sunday and the task to fit the capping wood.  This was positioned rebated and bolted into position.  Once bolted up Jake applied a coat of gloss.

    Apart from painting this completes the reversion.

    Next week should see the sheet fitted and of cause it is the GCR’s Winter Gala so TPO action for ourselves.

  • 02/01/19 – End of Year Review

    02/01/19 – End of Year Review

    The final day of 2018 and a visit to the Rail Innovation and Development Centre Melton.  More commonly known as the Old Dalby Test Track.  Those who have read our profiles will know this is where I work, So for me New Years eve was a day working,  for the rest of the team a tour and a run down the test track.
    2 full line trips buffer stop to buffer stop were made. One in 08 892 and the other in 47 714. 52 miles in total.

    On to New Years day and work continues on the Shockhood B. Advantage was taken of the extremely good weather with Jake priming the wooden batons made by Ross and exposed frame of the Medfit.

    Nick and I started the tarpauling bars for the Shockhood.  There were quite a few complicated bends, it was all figured out and after the sun had set both ends of the vehicle had received the end bars bent and ready to be linked.

    On to the review of the past year.  Having focused on the Brakevans these took a lot of our time so the vehicle total this year is lower, the numbers are as follows:

    4 doors
    2 re-roofs
    3 re-floors
    7 exterior repaints
    3 interior repaints
    5 seats reupholstered
    2 new vehicles
    1 Transit van starter motor
    23 new windows

    To finish I have written a poem, I hope you enjoy it.

    We started the year by re-wheeling a Shockvan
    A sheet was fitted to a wagon at Swithland

    Dummy shock gear was the focus of the day
    Until warmer weather when the fish came to play

    From white to blue it looked ice cool
    The first of three brake vans, they were cruel

    A shock van stripped of all but its doors
    A Midland box van we found its numbers

    An LMS Brakevan with 18 foot boards
    It received new upholstery, a new one for us

    A starter motor for a van but not one on rails
    The end of steam came but thankfully failed

    A work week in August and another brakevan fell apart
    That visit from Robert that pulled at the heart

    Despite the heat we focused on a stove
    Rebuilt the third brake, even got the doors to close

    It was time for some flats one from a Scottish works
    The other received a tank it could have been worse,

    A trip down to Gloucestershire to see Mr Stone
    Plenty of wagons were wanted but none came home.

    The war came to an end and a fire was lit
    A wagon arrived it was a Palbrick

    We ended our year with oil and pads
    Thanks to all our supporters Happy New year from the lads.

     

  • 30/12/18 – Merry Christmas and a Happy New Year

    30/12/18 – Merry Christmas and a Happy New Year

    Seasons greetings and our last post for 2018 and despite the festive season, Winter Maintenance continues:
    Axle Boxes, Pad Exams, Brake rigging inspections, and oiling, all vehicles in traffic have been attended to apart from those on the Mountsorrel Branch, as these were carried out by C&W Staff from Rothley earlier in the year. There are also 2 vehicles in the Dock at Swithland requiring Pad exams as the East side is currently inaccessible.
    Maintenance took us until Wednesday spread between Swithland Sidings and Quorn.

    Thursday attention turned back to the newly arrived Palbrick, The frames and the toolbox, which it arrived with, were sprayed with a Baking Soda mix to try and neutralize the rock salt that had been stored on the vehicle. This was worked in and a second application on Friday. So far things are looking good.  Nick also took some time to remove rust from the deck of the Sturgeon.

    Saturday and the Medfit received attention. It’s floor was no longer fit for this world so it was fully removed. The steelwork will require a few remedial actions before a replacement is fitted.

    As well as the Medfit our project to revert the Dace back into a Shockhood B has begun. The deck has been cleaned of Moss and Rust, as well as the space between the frame and body. Sunday and manufacturing the Hoop mounts was on the cards.
    Using the original mounting holes, mounting plates and a cover plate were manufactured.  These were installed at both ends and are ready for the hoops to be manufactured.

    Whilst these were being installed Ross began creating the wooden batons that run each side of the body,  under each lip.  This is made of 4 parts and is there to prevent damage to the sheet which will be fitted.20181230_125605

    We will be posting an end of year review on Tuesday and this will also include our exploits planned for New Years Eve as we visit another Railway.

  • 02/12/18 – Bricking it

    02/12/18 – Bricking it

    With S56010 essentially finished our attention has turned to a new arrival.  Joining us from the Bombardier works at Derby Litchurch Lane Palbrick B B462709.  This vehicle was purchased with the intention of becoming a chassis for re-wheeling a box van.
    This decision may be altered as an alternative use with commercial possibilities has come to light but this requires discussion with the GCR before we announce further.
    For now, the vehicle is being made fit to move on the railway.

    The first job was to remove all of the equipment from the deck.  This included the toolbox and what can only be described as the wheelie bin shelter.  During its life at Derby, it was in use as a match wagon and site domestic wagon,  for clean up and de-icing duties both track and walkways.20181201_143143

    My main task for Saturday was to address the step boards,  as can be seen above they have, at some time, taken a wallop.  As we are also reinstating the brake gear and to gain better access to the axle boxes the steps were shortened.20181201_143201

    This was carried out on both sides.  This involved removing the anti-slip coverings, shortening the boards and coverings then refitting said coverings.  I also had time to remove the east side footboard bracket as this was now redundant.

    At some point, the vehicle had taken a hit to the northeast buffer, this had pulled it away from the headstock.  The buffer was removed the area around the bolt holes that had deformed was heated and returned to its original profile.  The bolts replaced and the buffer refitted

     

    The south draw hook had also sheared. What was left was removed useful components salvaged and a new complete draw-hook fitted.

     

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    The other draw-hook at the north end was loose and missing a spring rubber.  This was undone and a new rubber fitted.  Of cause, the description of the work carried out is considerably shorter than how long it actually took.

    With the light fading, we began to look at the brake rigging. Most of the linkages and pivot points were sized.  A few choice applications of heat and penetrating fluid was liberally applied and attempts were made to free off the linkages to no avail.  The pivot pin for the missing brake arm was also removed.

     

    Final Job for Saturday was the application of the running number.20181201_163628

    On to Sunday and I completed the removal of the redundant Stepboard support.  As well as the remains of the Wagon clips.  After which I removed the bottom of the toolbox as this had become rotten as it was used to store rock salt I also scraped and cleaned the inside of the box.  This will be receiving a new wooden bottom and will be fitted to the wagon with an air gap below.

    Nick and Ross systematically freed off, removed, cleaned up and refitted all of the linkages, pins, and pivots of the brake rigging.

    Once complete our attention turned to fitting a brake lever and pin rack, we used the bracket on the W iron that held the footboard with a little adjustment.  It was heated, twisted and hammered into position. With the lever fitted this results in an operational handbrake, although for the time being only from the East side.

    The vehicle can now be moved, braked and can be identified. More to do next weekend.20181202_181012

     

     

  • 18/11/18 – Home Comforts

    18/11/18 – Home Comforts

    Having spent a week looking at images of SR Pillbox brakes my thought was S56010‘s stovepipe is too tall.  Although within the loading gauge we made the decision to lower it.

    Once lowered I applied heatproof sealant between the Outer Stovepipe and cast roof fitting and the inner and outer stovepipes, both externally and internally.

    Once this had cured we moved to a preservation first.  Since its arrival in 2005, the brake van has never had a stove. Having now fitted one we lit the first fire in at least 13 years.

    In the week I had purchased galvanized buckets, dustpan and “fire irons” for the van when I dropped these off I also added the earthing cable for the stovepipe.

    In the now warmed van, Ross and I fitted the ducket head cushions for the Guard.

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    To finish off Saturdays tasks the original stove pipe sign which was saved when the interior was dismantled was refitted in its original position.

    On to Sunday and the main task was the final fitment of all the upholstery.  Ross and I completed the east side cushions and I fitted the Guards cushions that fits above the main backrests and finally, all of the staples were painted black.

    The main cushions were also screwed into position from outside the duckets and the screw heads then painted by Jake.

    Whilst I had the black paint out I also added a BR(S) to the short circuit bar.20181118_142402

    The whole teams’ attention then turned to the fitting of insulation to the North end door.  During our test fire of the stove, we found if the door was left opened it started smoking.  So we added insulating material, steel covers and Jake primed them.

    One more morning of work left and then we need a new wagon to work on.  Next week you’ll find out which.

  • 28/10/18 – Did you set the clocks back?

    28/10/18 – Did you set the clocks back?

    As I stated in the last update I was on a week of earlies.  Monday I made a start on replacing the windows of S56010.  Unfortunately, there was only time to replace 5 out of the 6 vestibule windows.

    For the rest of the week, I have been carrying out work for Railway Vehicle Preservations as part of the ongoing preparations for Great War, Great Central on the 10th & 11th November. I have been Signwriting their Ambulance Coach in readiness for the event.

    On to Saturday and Nick and Jake in attendance, before the weather turned for the worse they were able to paint the headstocks of S56010.  The rest of the day turned to prepare for a number of future projects and generally tidying the sidings.

    Sunday and everyone on site.
    Ross and Jake started with spraying the Bogies of the Tankflat as I added the final detail, the fictional registration plate.  After the Remembrance event, this will be altered to more accurately reflect the vehicles 1942 origins. With these final details complete this brings a close to the repaint of this vehicle.

    Back on to the Southern brake and myself and Nick completed the replacement of the van windows I began on Monday.  Only one of the original panels remain as this was an original glass one still in situ and was easily cleaned up.

    Ross and Jake then joined us to add the external white details, Handrails and Lamp brackets.

    As can be seen below the vehicle is very much approaching completion and has come along way from the poor state the vehicle had reached.