Tag: ADB975397

  • 30/03/2025 – All Change

    30/03/2025 – All Change

    Hello and welcome to this week’s update. The Test Car has a new home and is prepared for the April event openings. The re-formed Mixed Goods returns to Quorn and we attend to a few repairs and maintenance items in readiness for the forthcoming Goods Experience Days.

    During the week the operations team carried out a large number of shunt movements that included extracting the Creosote tank and returning the tank train to Swithland along with a number of other wagons. The Creosote tank, being an engineers wagon, was transferred into the mixed goods formation along with the two Catfish and a vacuum braked Dogfish.

    Test Car 2 was also turned and re-positioned with the steel high ADE280364 at the buffer stop end of Road No.1. This will make the coach much more visible & accessible to visitors, and also make it much easier for us to manage visitor access when we open the coach on event days.

    The four box vans that still need some work to finish off the roof repairs were positioned in the yard and the mixed goods arrived into Quorn on Saturday morning.

    We wasted no time attending to the damaged vacuum brake pipes at both ends of the Dogfish DB993412, replacing the missing vacuum release chord and oiling up the brake rigging

    The power was connected up to the Test Car and we made a start on tidying and cleaning inside the coach. The deceleration meter mounting pad was also repaired and re-fitted to the steel high wagon.

    The vacuum brake test rig was transported down the yard and a brake test was carried out on the Dogfish in the Mixed Goods. Loose axleboxes on Mineral B550356 were also attended to and new split pins fitted.

    A cracked brake block on Catfish DB983393 was replaced. The replacement was swapped from DB983166 that’s currently handbrake only; this will be replaced in due course.

    Work continued on the chassis of tank 3606, concentrating on the end pocket areas at the south end, with more rust removal using hammer & chisel and the air needle gun. This was followed up with some carefully applied red-oxide primer.

    On Sunday it was great to see the re-formed Mixed Goods set in operation as part of the preparations and staff training for the forthcoming Goods Experience Days.

    More information about these forthcoming Goods Experience Days can be found on the GCRs website here: – Goods Experience Days

    There are also quite a few opportunities to visit the Quorn Wagon & Wagon team during April when we have Test Car 2 open to visitors at the following events:-

    Reunification Open Weekend – 5/6 April 2025

    Road Rail Steam – 19-21 April 2025

    Spring Diesel Gala – 25-27 April 2025

    Find us at the south end of the station yard at Quorn, just past the turntable.

    Pop in and see us for a guided tour of this unique piece of railway history, and find our how & why British Rail tested goods wagons. Keep and eye out for our Donations Lamp outside the Test Car; your support is very much appreciated.

    For more info about these events, and more, please see the GCRs website – https://www.gcrailway.co.uk/whats-on/

    Join us next week to see what we get up to during the Reunification Open Weekend; all the best, Dave

  • 22/12/24 – New projects…

    22/12/24 – New projects…

    Hello, and welcome to another update from Quorn. Now that the Catfish have departed Quorn destined for the Mixed Freight set, we’ve received the two TTAs, and the TEA has been brought down from the top of the yard. We’ll be looking at vacuum through piping these over the coming weeks and months. We’ve also been preparing for a short spell at Rothley to give the roofs of four of the vans some attention.

    First off, the team set about locating our 21″ vacuum cylinder spares, which were spread across a few locations. During this, the yard area was tidied up to release a complete (but not very well cylinder) from inside the Volvo’s bucket.

    This cylinder was removed from 3711 when it arrived, for obvious reasons. Now we are restoring a handful of engineer’s vehicles, which usually all have a 21″ cylinder, we felt that we’d need to check the condition of all available parts, which includes that cylinder…

    With a lot of brute force and occasional ignorance but without heat (surprisingly), the cylinder was dismantled. It remains to be seen if this cylinder will resurrect, but we can only try. Plus it gives us a chance to try soda blasting it!

    Dave removed the cylinder head from the de greaser and gave it a rinse off with the pressure washer. This was left to dry out in the heated mess coach. We’ll begin to assess the rest of the parts as time and other projects allow.

    As the light was falling, Dave and I took a brief look at the through pipe route for the three green tanks, the two TTAs having a well defined route in a bit of a contrast to the TEA.

    All that leaves us to say is Merry Christmas from us. We’ll have another update for you before the New Year with a bit of a wrap up and to cover what we’ve done over the Christmas and New Year period, do join us then!

  • 15/12/24 – A Lowfit at last!

    15/12/24 – A Lowfit at last!

    Hello all and welcome to this week’s update; after many years waiting we finally welcome the arrival of our Lowfit wagon into the fleet.

    Lowfit B452718 was built at Shildon in 1957 in Lot No.2729, to Diagram 1/002.
    It was last used on the main network at Basingstoke as an internal user wagon numbered 083473 and entered preservation in 2007 at the Mid Hants Railway.  The wagon arrived at Quorn during the week loaded with a D-type open container that had been constructed during preservation. Although the floor of the container looked quite rotten in places, our initial thoughts were to try and lift the container off the wagon in readiness for some necessary underframe and floor repairs.

    The Volvo was positioned and we attached some straps to the lifting eyes; gently raising the forks however pulled two of the lifting eyes straight out of the framework; it was somewhat more rotten than we had realised.

    So onto plan B; we decided to dismantle the container in situ on the wagon. Whilst the floor and side framework was rotten and not saveable, the side panels, corner framework and doors were quite solid. With most of the team on-site on Saturday things happened quite quickly, the doors were removed, end panels unbolted from the sides and the parts lifted from the wagon onto the Volvo forks for moving to storage.

    The remainder of the rotten framework was swept off the wagon and disposed of with the help of Hector and his trailer.

    The south east corner door frame of the Lowfit, catch pin and loop had taken a bash at some point in its life.  Ernie got out the gas bottles and heated up the bent loop which was straightened with Nick’s favourite item from his toolbox. Once cooled the area was treated with re-oxide primer.

    With most of the team on-site Mark treated us to some fabulous turkey & duck Christmas baguettes for lunch, thanks Mark and the chefs helpers.

    Further progress was also made on Test Car 2s generator; Ross and myself drained the coolant out of the engine, removed the rocker shaft, the cylinder head, and finally got to the bottom of the poor starting and lumpy running. The cylinder head gasket had totally failed between cylinders 1 and 2.

    The cylinder head studs were removed from the block and surfaces cleaned, cylinder bores cleaned & hoovered out, checked for condition and the engine set to No.1  piston at TDC.

    On Sunday myself and Ross dismantled the cylinder head removing the cam followers and valves; the large pillar drill made an excellent valve spring compressor.

    The cylinder head was then soaked in a bath of warm degreaser solution and as much of the gunk removed as possible. Further cleaning up is planned for next week.

    The repaired corner on the Lowfit was given a coat of gloss Bauxite.

    The two Catfish wagons are planned to leave Quorn next week, in readiness we completed a vacuum brake test on both wagons, finding a slightly suspect vacuum cylinder branch pipe on DB983393 which was duly replaced.

    Thanks for reading, join us again next week, all the best, Dave

  • 08/12/24 – Keeping Busy

    08/12/24 – Keeping Busy

    Hello and welcome to a very wet weekend update from Quorn. The Test Cars’ generator continues to be problematic; however we have completed the outstanding mechanical item on one of the Catfish.

    During the week I was asked by the Rothley C&W team if I’d help out with part of the signwriting on BG 81382 which was being finished off ready for release from Rothley and use on the Santa Special trains this weekend.
    (Photos courtesy of & copyright Jamie Swanson)

    Mark, Tom and Charlie got stick into some interior cleaning in Test Car 2.

    Whilst Ernie did some repairs to some of Test Car 2’s 1980s vintage wooden chairs.

    Under Catfish DB983393, the initial thought was to heat up the area surrounding the two sheared bolts and use an easy-out extractor to remove them, however the bolts would not budge. So Ross and myself moved on to plan-B and drilled out the two bolts and tapped the holes for M12, then secured the saddle back into place.

    With a fully charged starter battery connected to Test Car 2’s generator we were hopeful to get it running again. After quite a few attempts it finally fired up, however it was not running very smoothly at all and didn’t sound quite right either. We tweaked the fuel pump adjustment and tried again, but it ran much the same.
    Our conclusion after all the replacement parts and checks we have done is that the problems could lay deeper in the engine; so we have decided the next step is to check the state of things in and under the cylinder head. The first task being to remove the exhaust.

    With the exhaust manifold removed it became clear that that this engine needs some further TLC. The exhaust ports being very badly coked up.

    We continued to remove parts in readiness for releasing the cylinder head.

    Thanks for reading. join us again next week, all the best, Dave

  • 01/12/24 – Wash and brush up

    01/12/24 – Wash and brush up

    Hello everyone, and welcome to another update from Quorn. We’ve been able to progress a few jobs this week, with mechanical work culminating on the Catfish, the GUV has had another coat of paint and the coaches have been cleaned.

    Continuing the progress on the GUV, the last few patches of GUV were cleared back to bare metal, then sanded and primed. Dan, Ernie and Tom concentrated on fixing the loose body side rubbing strips.

    Reflecting the fact that the Catfish are cosmetically finished, Nick got them ready for a vacuum test by fitting vacuum hoses. We had also made a start extracting two sheared bolts in the hopper door on DB983393, which need to be extracted to refit one of the door mounting saddles.

    I continued looking at the generator and replaced the starter solenoid and double checked the timing, hoping I’d find the cause of it not running, sadly at the end of Saturday this was not the case, but I put the battery on charge for the night.

    The rest of the team made good progress and got the west side of the GUV covered in undercoat, ready for a coat of maroon gloss when the weather allows.

    Sunday’s weather started on the wet side. Mark and Tom did the usual gutter clearing, after noticing the water running down the side of the two coaches. After the worst of the rain, the pressure washer was used to jet the gutters, after which the coaches were cleaned using a bit of snow foam. On the west side a look out was used to ensure the group were away from the running line.

    I did a little bit more on the generator and got it running, which is a huge step given were we were with it some time ago. There is some fettling to do with the idle speed and fine tuning of the timing before we can put this back into use.We are starting to look at some improvements to the generator like an electric lift pump and maybe an alternator instead of a dynamo.

    We’ve ended the weekend with two clean coaches, a running generator and the GUV in undercoat on the west side. We’ll see what the weather brings next week, but we should are looking at completing the mechanical work on the two Catfish and hand paperwork over the Carriage & Wagon to begin their acceptance. Thanks for reading!

  • 24/11/24 – Hiding from the weather

    24/11/24 – Hiding from the weather

    Good evening all, and welcome to another update. With the Catfish finished, and the weather taken a turn for the worst we’ve looked at inside work, though the GUV did get a bit more attention.

    I concentrated on re-assembling the genset in the Test Car, bleeding the fuel system, replacing the coolant and of course trying to start it. Sadly, still no joy with getting it running so still more work to do on this.

    In a gap in the weather on Sunday, the Baldwins managed to get some more of the west side of the GUV stripped back and prepared.

    Thanks for reading! Fingers crossed for better weather next week, join us there and see what we get up to.

  • 20/10/24 – Keeping ourselves busy

    20/10/24 – Keeping ourselves busy

    Hi everyone, welcome to this weeks update from the team at Quorn. The weather has hampered our plans to get some paint on the Catfish; however we’ve kept ourselves busy.
    Some stock positioning shunting too place whilst we continued with progress on the LMS brake van, some more items on the to-do-list and Test Car 2s generator.

    During the week Tom, Dan and Nick continued with painting on the LMS Brake Van M730562 at Rothley, handrails, lamp brackets, swan necks and underframe were progressed. A new step board was also made and fitted.

    The new paint arrived ready for the two Catfish wagons, however the inclement Saturday morning weather meant that wagons were too wet for us to apply any paint, so Oliver made sure it was stored away safe.

    The old crank pulley oil seal was removed from the timing cover from Test Car 2s generator; the cover was then de-greased and pressure washed.

    A new seal was then fitted using a suitably sized drift and our makeshift press with a final knock-into position with a hammer.

    Hector’s cab parts were loaded onto one of the box vans for safe keeping and we sorted out some spare bolts in readiness for box van repairs before the Class 37, 37714 arrived to manage various shunt moves at Quorn for stock positioning.

    Ross and myself continued with cleaning up the timing cover mating surfaces on Test Car 2s generator, and repairs to some of the generator wiring.

    Richard resurrected some old skills in repairing and servicing two of Nick’s 1970s record players.

    Ernie and Nick installed a lighting power supply cable across to the Fish Van on the dock; this will help us as the nights draw-in.

    Mark, Tom, Oliver Dan and Nick managed to a bit of house keeping in the short spell between the Sunday morning rain and the lunchtime rain. The rotten sleepers were moved from the dock to the wood pile for the bonfire.

    A general tidy up of the area on the dock and some gardening will help improve the access for vehicles to the dock.

    Thanks for reading, join us again next week.

  • 13/10/24 – Ticking things off the list

    13/10/24 – Ticking things off the list

    Hello everyone, and thanks for joining us for another update from Quorn. The autumn weather is definitely settling in, so we’ve been ticking jobs off the back burner list. During the week, Dan finished the signwriting on the LMS brakevan, which now leaves some underframe painting to finish.

    With rain predicted on Saturday, I started looking at re-assembling the genset in the Test Car. Naturally, I started by taking it apart more… To re-attach the fuel pump, I wanted to check the timing on the geartrain, so ended up draining the coolant from the system and removed the radiator and water pump to gain access to the timing case. As I was removing components, Charlie took them outside and cleaned them with the pressure washer.

    Nick and Ernie took a look at the drawer in the kitchen on the coach, which has been broken for a few months. The drawer was re-assembled with additional L brackets to re-attach the front of the drawer. Back in the generator room, I found broken wires on the magnetic pickup and the dynamo, which may have contributed to the issues with the generator.

    On Sunday,we started by moving the barrels from E281882 back into B765272 to put them back into covered storage after Railways At Work.

    We then moved onto some light landscaping, to clear an access ramp to get Danny up onto the dock to help in clearing that up.

    I went back into the Test Car and finished piping up the fuel system, which leaves just the control actuators and the cooling system left to re-assemble. I also repaired the intermediate cover which had some loose rivets.

    The light landscaping turned into heavy landscaping to fill in some of the ramp way to make it less steep for Danny, who eventually made it onto the dock.

    Dan and I went to test the air brakes on the TEA tank, however part way through the test, it was found that one bow girder was not moving when the brakes were applied. We stopped the test and sent Dan under to lubricate and tap the linkages to free them. This didn’t remedy the seizing this weekend, so we’ll look at it again another time.

    Thanks for reading! we should be back on the Catfish next weekend, weather permitting, to apply the black paint. Joins us then!

  • 6/5/24 – Bank Holiday Bauxite

    Hello everyone and thanks for joining us in this bank holiday update. Unusually for a Bank Holiday the weather has been glorious so we’ve applied some paint to the Palvan. During the week, Tom and Oliver sanded and primed the ends of the van.

    Dave and Barry took a look at the Test Car’s generator. Barry and Dave undertook a compression check on each cylinder, then re-fitted the injectors and tried to start the generator. Sadly no joy due to a failed start battery so this was removed and charged to try another day. From what we could do, the generator doesn’t seem any more likely to start, so now suspect the fuel injection pump has failed.

    While Ernie undercoated the wood work on each end of the Palvan, Nick and I finished off work on A1610B. The last corner was looking rather frilly so had a piece of steel cut and sandwiched over the top. This was drilled and the corner bolted back together. Having lost the battle with the generator, Dave took to scraping the container, Charlie also having a go at this.

    On Sunday, Tom, Oliver, Dan and I applied some gloss to both set of doors on the Palvan as a first coat. Oliver and Tom also applied gloss over the undercoat applied by Ernie on each end. Some of the lads carried on with the needle gun on the Palvan chassis which quickly ran out, so they moved onto one of the Catfish. Nick concentrated on patching the container with Mark.

    Nick and I concentrated on the south end metal work, myself with the needle gun, being very careful not to catch the wood work while Nick followed me with a scraper to catch the edges. We each got a bit of primer and primed our handiwork, which completed the work this week.

    Next week, we’ll tackle the north end of the van and get the into primer, and maybe the other end into undercoat. Join us then to see how we get on!

  • 26/01/20 – Winter Gala

    This weekend has of course been the GCRs winter gala, we stepped away from Rothley and ADB977107. To open the doors at Quorn and allow you to see what we do, see Test Car 2 and Madge.  It was great to see so many of our followers and supports and thank you for taking the time to come and see us.20200126_121242

    Work, however, did not stop.  Nick, Ross, and Jake re-floored E280364 and changed the few rotten planks on E281882.

    Dave and I along with Eddie and Harry played hosts for our visitors.  Dave explaining the Test Cars past and I demonstrating some signwriting, namely the W.H.Smith & Son wording for the kiosk at Loughborough83421767_1095605867498752_7962423583538413568_n

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    Once the floors had been completed Nick, Ross and Jake then moved on to the overhaul of the 15″ vacuum cylinder from B385782.20200125_141559 Sunday and an unscheduled visitor into the yard, namely 46521 deputising for 4953 which had failed that morning. We took advantage of the vist and had the Iron Ore tippler moved to the centre road so we could fit the 15″ cylinder before we opened the doors.

    Once the loco had left the cylinder was placed back under the Tippler and the doors of the test car opened.

    A vacuum test was carried out after a hose change and the vehicle deemed to be fit, just awaiting better weather to complete the vehicle.

    Madge was on display and had the opportunity to make some friends on the few trips around the yard.

    The sign painted Saturday was cleaned of chalk and will be collected next weekend to be fitted to the Kiosk at Loughborough20200126_193937

    Jakes final task was to clear the build-up of moss from inside the tippler and in due course extra drain holes will be being added to the wagons floor.20200126_152036

    Finally, for this update a few views from the gala the visiting NER petrol although Diesel-powered rail car and our van train “plus” including Shochood B and Loaded Conflat.image5

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