Welcome to a sunny June weekend update from the team at Quorn. This weekend we’ve been doing some heavy metalwork on the Catfish and finishing the last few jobs on Palvan B781908.
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Saturday started with Tom and Dan doing some oiling of the brake rigging on the Palvan.
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Oliver helped Nick replace the vacuum brake hoses on both ends of the Palvan.
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I removed and tested the fuel lift pump on the Test Car; all was good so this was re-fitted.
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Ernie and Ross concentrated on cutting, welding and grinding of some more of the gouges imparted by digger buckets on the Catfish DB983560.
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Thanks to Mark for bringing along some provisions for a BBQ lunch; prepared by head chef Oliver who was helped by sous-chef Charlie, and of course Tom (being a Grade 6 food techie) had to supervise.
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After lunch there was some more cutting, welding and grinding.
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The Test Car’s cannister oil filter was also removed and cleaned out.
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Then there was some more welding and grinding.
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Sunday and more sunshine; Ross fitted a few missing split pins that we noted during the previous wagon inspection we did on the Palvan.
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I did some measuring up in readiness for preparing the templates for the forthcoming signwriting on the Catfish wagons.
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Nick, Ross and myself then got the vacuum test rig started in order to look into the train pipe leakage problem on the Palvan.
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The vacuum hose end seal on the south end was noted to be leaking so that was replaced.
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A small leak was found on the cylinder piston rod gland so that was removed and inspected; the seal was slightly damaged so this was replaced. It was also noted that the cylinder release was not a smooth or as quick as it should be. On closer inspection the piston rod itself was seen to be slightly bent, so a ‘straight’ replacement from stock was cleaned up and fitted.
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With the leakage problem and slow release still persisting we decided to drop out the inner cylinder and piston to check the ball valve and rolling ring.
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The rolling ring was inspected and noted in very good condition, therefore it was re-fitted to the piston. Some muck was cleaned out of the ball valve and a little dust in the inner cylinder hoovered out before refitting back into the cylinder dome. The die-nut was run down a couple of the dome cover stud threads and one stud re-fitted further into the dome. The release valve was also swapped for another overhauled one.
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A replacement hose for connecting the test rig to the wagon was fitted as we noted some collapsing of the old hose. The branch pipe clip was also replaced with a slightly smaller one to try and get a better seal here.
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Finally we managed to achieve a respectable vacuum train pipe leakage rate for the Palvan.
This completes our restoration work on B781908 which started back in November last year; here’s the before and after. The wagon will now be handed over to the Carriage & Wagon Department for final inspection and sign-off; however we will also carry out a running assessment / inspection during its in-train first operation.
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Thanks for reading, all the best, Dave
Congratulations on completing the Palvan restoration. Have been following you for a year or two now and compared with the previous tasks undertaken during that time this definitely seems to have been a mamoth task and the completed product looks fantastic.
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