Author: rloades109

  • 11/03/2019 – Framed again

    Good morning everyone, and welcome to another update from Quorn Wagon and Wagon.  This weekend, we have continued to work on the LMS box van.  At the end of last week, we had stripped the side from the van and removed the door frame for patterns.

    On Saturday morning we took delivery of the new side planks for the van from Harlows timber merchants. These planks have been pressure treated, so should stand up to the beating the weather throws at the body sides. We also took delivery of a new sliding door frame, ably carried by Matt and Nick.

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    So the day begins, we began by building up the door frame with all the bits of steel framework to enable the door to be refitted to the van. Taking advantage of the good weather, Matt and Nick set up shop on the dock. Before mounting anything to the frame, areas where things were to be mounted had a generous coating of wood primer. A tea was consumed to allow the paint to dry a little bit, and then the top and bottom angle irons were fitted.

    Then the side frame was added, which governed the placing of the rollers at the top of the door, and the corner reinforcing pieces at the bottom.

    What was I doing whilst Matt and Nick were readying the door? I was repairing some other doors, as fitted to another Transit van. I replaced locks on the load space doors, and then sat in the warmth of TC2 and repaired the rear door wiring loom. Once I’d fixed the central locking, I assisted Matt and Nick with the rehanging of the sliding door. We’d managed to slide the door on, but some adjustment was required to allow the door its full range of movement. Last thing to fit to the door was the latch.

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    Just before hometime on Saturday,  Matt painted the door frame and rebates in wood primer and part of the side ‘fell’ in.

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    On to Sunday. Before I had got there, Matt and Nick (in between perusing the Swapmeet) had fitted the south side planks. Both end required a filling strip, at the top of the cladding, which I set myself up in the GUV to make. These were slid in, and then a team of Dave, Jake, Matt and Nick set about bolting the side planks and internal cladding to the van side. Whilst they did that, I cut out the plywood back piece for the sliding door. The vertical front planks screw to this backing wood, so this task readies us for next week.  Nick, using the angle grinder, cut off the end of the bolts that were considered too long, whilst I was inside screwing the backing boards to the door frame. Now the sides are in its a bit dark in there! Jake finished the door off by painting the front face of the plywood in wood primer.

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    Next week, the door planks will be added and the side planks painted with wood primer (weather dependent). Then onto the other side!

    Thanks for reading!

  • 24/02/2019 – Getting Ready…

    Welcome to another weekend update from the team in Quorn, featuring some unseasonably warm weather! This weekend we have started to come back to normality, back in our pen in the south yard at Quorn. During the week Test Car 2 and the CCT were stabled back in the Up Reception South (thanks to the Ops team), with the Yellow Coach being taken to Rothley for its much-needed bodywork repairs, courtesy of Jamie and Pat at Rothley (Thanks in advance guys!). More on that will be covered in later updates.

    This weekend has seen us get ready for the coming year, with stuff being tidied and shifted around (yet again!). Having the CCT delivered has meant that we could empty the ex-Windcutter Group stores van, M500954, as well as move some items from the GUV.  The LMS van begins its journey through a reclad and repaint for it to join the van train. The intention is to refit the vacuum to this vehicle, which we are beginning to sort out components for.

    As the CCT is no longer being retained for as the fire van, we carefully removed the IBC cubes and relocated the firefighting equipment to one end of the van. This allowed us to transfer all items from the LMS box van into the CCT. Once all items had been removed, Jake started taking down the internal racking, which has been retained for redeployment; after all, we can’t let things go to waste!

    I assisted Jake with this, once I had replaced the front bumper of my car, which had sustained some damage from a Muntjac deer one Saturday evening last winter.

    Also on Saturday, as part of some fireman training, the box van train had several trips, which saw the use of the Southern brake van, which was also removed from the South Yard during the week.

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    Sunday morning rolls around, and with it bring us a special guest! We were pleased to reunite Dave Bower with Test Car 2. Dave used to work TC2, among other vehicles, during his time working for British Rail Department of Mechanical & Electrical Engineering from 1983 to 1994, and then for Serco until 2008. In this time Dave was involved with over 700 tests on new build vehicles as part of their acceptance to the network or investigating modifications to existing vehicles. Dave has also written a fantastic book, Rail Vehicle Testing (link on our Links page), which details the tests of which he was a part of,  why vehicles were tested, and information about the Test Cars among other subjects. Dave was able to show us how the coach worked, and some finer details of its conversion (including any questions we had) and told us a few stories of his time working the coach. Thanks for coming along Dave, and we hope you had a good day; as we certainly did!

    Other tasks undertaken today included reuniting parts of the tank with the tank, and finding and cleaning a fridge to use in TC2 whilst the Yellow Coach is away.

    Next weekend, we plan on starting to strip down the dock side of the LMS van in readiness for its reclad; and we shall continue to tinker with Test Car 2. Thanks for reading!

  • 10/02/2019 – QXA to QXX

    Welcome to this weekend’s update from Quorn Wagon and Wagon’s Rothley outpost. We have again been working on Test Car 2, in preparation for its move to Quorn as our temporary base.

    Work this week has concentrated around the vehicle’s vacuum system. Last week, we were able to prove that the vacuum pipe was intact as a throughpipe. We started off by digging out some spare Direct Admission (D.A) Valves and sections of specially shaped pipework out of the van train from storage. This pipework fits into the tee joint from the main vacuum train pipe and drops them down to the D.A valve bracket next to the Vacuum Cylinder.

     

    Firstly, We removed the bungs from the tee pieces in the train pipe and connected the first section of downpipe to the Crane coupler.

     

     

    One end had a frame fitted to carry a DOPLAR speed measuring system whilst it was based at the Old Dalby Test Track. Matt set about removing that frame whilst Nick and I trial fitted the down pipes to see where the bracket would sit. This would also show us modifications we’d have to make to the pipework to be able to fit with appropriate clearance for all components in the area.

     

     

    Both ends required no modification to the down pipe, but both had to have the mid section and final sections altered to allow for best positioning on the coach.

     

     

    The electric pipe threader made light work or altering the pipes and by the end of Saturday we had managed to effect a brake application on the North end of the coach.

     

     

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    We found that whilst the brake applied satisfactorily (first time since 1991) they would leak off after 5 minutes. we cleaned and exercise the release valve on the cylinder. This resulted in the cylinder holding for 3 hours, after which we lost interest. Our attention then move to the south end brake cylinder.

    The south end of the vehicle is fitted with reduced diameter cylinders on both the vacuum and the air braking system.  This means that the vehicle has a reduced brake force reducing the risk of the wheelsets locking up as this end was fitted with tacho counters for distance measuring during tests. We found that the brake cylinder again applied well, but released after only 1 minute. Initially, we suspected the release valve, so changed that for a spare. this did not rectify the issue, so we then replace the DA valve. This hasn’t rectified the issue, so no the cylinder is suspected. This will be replaced in due course. Matt remains confident in the air brakes of the coach, after its final movement to the loading pad on the Test Track.

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    Work didn’t just take place on the brakes. Matt has trimmed the buckeye chain guide to allow the Brake Pipe cock on the air system to latch shut. I reinforced the door frame around the lock I fitted last week. I also noticed whilst underneath the vehicle that the return spring for the south brake rigging had come adrift and was not in place. A spare was found and Matt wedged himself into the bogie and fitted it. The train lighting jumper blanking cover was found in the guards area, so Matt refitted it to the North end from whence it came.

     

     

    Thanks for reading this update, join us next week, when the saga of the vacuum cylinder continues!

  • 27/01/2019 – “I’m Postman Matt and no, I don’t have a cat!”

    Hello everyone, and welcome to another weekly update from Quorn Wagon and Wagon.

    This weekend has seen the railway host the annual Winter Steam Gala, with the van train running and the mixed freight making a welcome reappearance. We were also staffing the demonstration Travelling Post Office train, performing ground duties in the mornings and staffing the train for the afternoon run.

    Most importantly though, we fitted the sheet to the Shochood B, which makes us the proud owners of the only Shochood B in preservation! Matt collected the sheet on Friday. We have fitted it temporarily, as the best place to store a sheet is in place on the wagon. The sheet will be removed before painting. As the fitment is temporary, we’ve used cable ties to attach the sheet to the wagon. We discovered when putting the sheet in position, that one of the bars was able to jump off its prop, leaving a sharp pole. Nick and I went around inside the wagon and used some steel strapping to prevent the poles lifting off the poles.

    Matt has put some effort in and put himself together a GPO uniform to play the part of a postman from the 1960s. He also borrowed a post bike from the station to complete his image. On the TPO, Matt and I did some work to free of the letter flaps, as fitted to Postal Sorting carriages.

    Thanks for reading this small update, and join us next week for another!

  • 13/01/2019 – Winters are for Westerns

    13/01/2019 – Winters are for Westerns

    Welcome to another update from your friendly wagon bashers at Quorn. We have again been busy reversing the Dace conversion on the Shochood B. With all four of us in attendance plenty has been achieved. During the week, Matt has placed an order for the sheet as fitted to these vehicles, so in 10 days from now Matt goes and picks the sheet up, and that next weekend we fit it. An exciting development!

    Saturday saw Nick and myself using our best carpentry skills to make more capping wood for the east side of the body. This wood prevents the sheet from being worn away by the edge of the angle iron at the top of the body. Once we’d cut and shaped these, Jake got the wood primer out to give them a coat. Jake also gave to capping wood made previously a coat of undercoat. We plan to get these ready to go back on the wagon with a few coats of gloss all over. This should help to protect the wood from rotting so quickly.

    Meanwhile, Matt had begun one of his personal missions; to reinstate the handles to the South West and North East corners of the body. During conversion, these handles were cut off and welded to the end to act as grab handles for the coal hopper style steps fitted during the Dace conversion. Matt began by cutting the handles off, and matching them to their positions on the body. As we have no welder, and an insufficient power supply (a 16A cable) to run one, we couldn’t reattach them with welds as was original. We’ve been somewhat creative and used bolts through the body to reattach the handles. This involved drilling through the nub of the handle left, the body skin, and a few partition slot guides. We also drilled and tapped holes into the handles to receive M12 bolts.

    Once Matt had finished fitting the handles, he finished the corrugated end by removing the nub of the handle and grinding it flush. Jake was then let loose with the red oxide primer to give it a coat before we begin painting in the better weather.

    Due to the weather at the start of Sunday, we began the day by tidying up and clearing out one of our storage cupboards in the Mess Coach. The first class toilet, long unused, had become a dumping ground for old Hi-Vis and various other items. This has been cleared out in anticipation of works to the coach.

    Matt continued his role as our resident Time Team expert by beginning to sand down the bodyside of the Shochood to find its regional allocation and if it had any branding.

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    The weather had cleared so Matt continued his handle relocation scheme. Nick, Jake and I started to remove the rust that has built up between the body and underframe. This has built up due to the shock capability being removed, thus the body not being allowed to shift, which would have broken up the rust.

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    Matt’s second personal mission of the weekend was to relocate the lamp brackets back to the body. This only leaves Matt one mission in our reversion of the Dace conversion; removal of the coal hopper style footsteps from the body end.

    That finishes this week’s installment of the quest to have the only Shochood B in ‘original’ condition in preservation. Join us next week for another (exciting?) installment!

  • 06/01/19 – Hoodwinked

    06/01/19 – Hoodwinked

    Hello everyone, and welcome to another update from Quorn Wagon & Wagon.  This weekend started with Nick, Jake and I continuing to manufacture the sheet hoops for the reversal of the Dace conversion. Unfortunately, Matt had to work, but popped in after his shift had finished.

    On Monday,  Nick and Matt had manufactured the upright sections of the sheet hoops, which only left the horizontal sections which Nick and I manufactured and fitted today. The steel tubes we had rescued were in 11ft sections with a foot on one end. The foot was cut off with the angle grinder, and the end dressed. To join the bars, Nick had found some surplus steel pipe at Rothley to act as an internal sleeve. These sleeves were cut to length and ‘gently’ persuaded into the hoop tubes. We decided we should bolt the sleeves together to prevent the internal sleeves sliding into the outer hoop tube when assembled.

    Whilst Nick and I were playing with hoops, Jake continued priming the chassis of the Medfit.

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    Once completed he assisted Nick and me with fitting horizontals to the hoops irons. Before lunch, the top hoop was assembled and fitted to the wagon. Jake had to go to fill his face at a friend’s birthday party, and Nick and I went to assist the Ops Team/Carriage & Wagon by removing a TSO requiring repairs from the passenger train using Rothley’s resident Class 10.

    Upon returning, we continued assembling the two side hoops. Matt arrived while the last joint was sliding together on the final hoop. We had a swift cup of tea and set about positioning the hoops as they would be under the sheet ready for Matt, Nick, and Jake to finalise and fix the positions tomorrow. Matt will continue the report tomorrow as I have to pilot a misbehaving car back home.

    On to Sunday and Jake moved back to the Palbrick, clearing out and tidying the drag boxes.  These were full of rust, moss and detritus.

    Nick and I (Matt) continued with the Shookhood hood bars.  Looking at images of this type of vehicle from the 60s and 70s it’s clear their long length posed a few issues. Many are not level and a fair few are sagging in the middle.  As this vehicle is for demonstration purposes we have taken the decision to support the bars at strategic locations to maintain the level and prevent sagging once the hood is fitted. The supports were bolted to the steel floor.

    Once the sheet has been made and fitted these supports will no longer be seen and as the vehicle travels the railway the bars will remain in a fixed location.

    Any protruding item that would risk rubbing and wearing down the sheet was trimmed, and the all-important measurements were taken to have the fitted hood manufactured.

    Ordering the sheet is my task for the week and by next weekend hopefully that order will have been placed.  we shall see what next weekend brings……………….

  • 23/12/18 – Wonderful weather… for shark spanners!

    23/12/18 – Wonderful weather… for shark spanners!

    Welcome to another update from us lot at Quorn. This weekend has seen routine maintenance take place to the running fleet.

    We keep records of the work carried out to our vehicles, and perusing these records showed us that the all vehicles are due a routine pad exam. Whilst undertaking the pad exam we also take the opportunity to oil up any pivot points in the brake rigging, so that whatever brakes are fitted remain operational. On both Saturday and Sunday, we worked on the vehicles stored in Swithland Sidings.

    On Saturday, we performed pad exams on the van train. This also included the LMS brake van which is currently running on the south end of the rake.

     

    After we’d done the pad exams, we rattled down the van train oiling the brake rigging and oiling any screw couplings. This also included the B954268, which was stabled next to the van train on the south end of the mineral rake.

     

    Sunday saw some of the currently disbanded Mixed Freight, and a Rudd, get the same treatment as the van train. We also corrected a failed attempt to fit the Bogie Bolster D with a new vacuum hose, on its south end. This had been secured to the wagon with Gaffer tape, instead of using a hose clamp suitable for the diameter of the hose. Had this been brought to our attention and the consumable parts supplied, we would have happily fitted the hose. Hopefully, the rectification of this should see the vehicle back in the mixed freight. Matt also fitted a sign to the interior of B954268 which is the final detail in this brake van.

     

    We began oiling once these small jobs were complete. Today, we have oiled the tank wagons  (3436, 6581 and 998926), some of the open wagons (E281882, E301588, B385782, B425356, B550356, B721587, B724570, B732357 & B740654) and some of the Departmental fleet (DB972018 and DB928135). Not all of these vehicles have plain bearings, which means some of these had their rigging oiled only.

    Tomorrow, see us back at Swithland completing the open fleet, and starting pad exams at Quorn! Thanks for reading!

  • 16/12/2018 – Odd jobs

    16/12/2018 – Odd jobs

    Saturday comes around once again, Matt is unfortunately at work and Jake is gorging himself on a Festive Scout camp.
    Work continues on Palbrick B (B462709) to make it fit for movement. Last weekend, We had managed to remove 2 broken brake block carriers and had identified a 3rd to be changed. Armed with 3 replacement carriers, Nick and I set to work refitting the ones that had been removed, and replacing the last one. The final one was replaced due to the lower corner being broken off.

    I also refitted the air brake pipe cocks and hoses, so that now the wagon retains its air through pipe, although these now require to be painting white. When more is known about the wagons future we may reinstate the vacuum system.

    Once the brake blocks & carriers and the air pipes had been refitted, it was lunchtime! During lunch, the heavens had opened giving everything a good soaking, so Nick and I spent the rest of the day tidying in our tool van and workshop vehicle.

    On to Sunday and Matt continues this report.

    First job and running maintenance on the Southern brake van.  This entails oiling of the brake rigging and pad exams.


    One of the pads was found to be worn and this will be replaced in due course although it requires at least 24 hours soaking in oil before the replacement pad can be fitted.20181216_104940

    Once this was complete Nick continued tidying the tool van.  Whilst I began “stitching” posters together.  These are for the station at Quorn and unfortunately, I can only print up to A3 so for larger posters, and not wanting to have them professionally printed for additional cost, I glue sheets of paper together.  To see the full range of posters visit Quorn station from Boxing day.

     

    Time was also taken to update the vehicle record cards, every vehicle we have has its own series of cards that detail all the exams and work that has been carried out.20181216_135312

    Finally, our attention turned to our potential next project.  Dace B726344.  The intention is to restore the vehicle to its Shockhood B condition,  these vehicles were fitted with foldable hoods and this will be reinstated.  Nick took time to remove the moss and loose rust from the floor whilst I took measurements and began planning the installation of the 3 foldable hood bars.

    Next weekend our attention will be turning to routine maintenance with such a large fleet this is essential to keep them operational.

     

  • 09/12/18 – Feeling hot hot hot.

    09/12/18 – Feeling hot hot hot.

    Saturday begins, and work continues on the new arrival; Palbrick B462709. I didn’t manage to take any pictures, as Nick, Jake and I have been quite busy continuing to get the wagon fit to move. Matt was attending the Quorn Station Christmas Doo

    It had been brought to our attention that the vehicle was prone to derailment. As with all vehicles we work upon a thorough inspection is carried out.  We have attributed the vehicles poor running to a number of factors:

    1. The brakes had been seized in close proximity to the wheels restricting rotation under certain circumstances 

    2. The majority of the track at Litchchurch Lane is buried so the wagon, being light, is likely to ride on top of any obstruction of the flangeways

    3. At one end, the W-irons are not vertical and are forcing the wheelset in one direction.  Sat on straight track the wheelset is not sitting centrally and is hard up against the flange of one side with both irons pushing against the axle boxes

    All of these factors add to the likelihood of a derailment. As a matter of cause, we have lifted the wagon to be sure that the axle boxes slide up and down in the horn guides, which they do freely but we will address the W Iron issue.

     

    Today also saw the Eastside handbrake fitted. The eagle-eyed amongst you will have read that last week we fitted the east side handbrake. The vehicle was turned in the week during work for the testing contract in Quorn South yard. The fitting of the handbrake was quite involved as we had to use the ‘hot spanner’ to adjust the handbrake rack so that the holes for the handbrake pin would line up. We also had to align the holes to mount it to the wagon, activity that continued long into the darkness.20181208_172015

    On to Sunday and it is Matt that continues this report. 

    Returning Sunday and straight into straightening out the W Irons.  Using the “heavy hammer” AKA a Volvo L70.  Pressure was first applied to the North West iron. The pressure remained and the top of the iron heated allowing it to relax into the more favorable position. This was repeated on the North East corner although the iron was pulled with heavy duty chain and again heated and allowed to relax.

    The result is a full set of straight W Irons one in each corner.  Again the wagon was lifted and the axle boxes proved to move freely.

    Next job and the removal of the seized brake block carriers.  Despite successful removal they were in a poor condition and are not fit to be refitted.

    This once again leaves the vehicle without brakes so it has been coupled to a Grampus and next week once spares have been recovered it will be reassembled.

    The brake pin racks were also fitted with pins.20181209_161804

    I also did my time team bit and revealed the original running number.20181209_123213

    S56010 is also absolutely complete and once the point is back in can be released to traffic.  The last job completed was the fitting of filler pieces in each corner of the bodywork which was sealed and painted.20181209_162432

    I shall also add some images of the fully refurbished interior and those that remember it originally will notice the changes.  Unfortunately, we didn’t take any images before refurbishment but it was extremely work worn.

     

  • 25/11/18 – Don’t get hooked up on that!

    25/11/18 – Don’t get hooked up on that!

    This weekend has seen work on the Southern brake van (S56010) very close to completion. Next week should see the van ready to leave the yard.  On Saturday, I began the day by making running repairs to a new acquisition of Nick’s.

    Whilst I was doing this Matt painted the handbrake standard, stove surround, earth strap and vacuum setter handle in black gloss. This concludes the work for the interior of this van. Matt then went on to manufacturer a chimney cowl for the stove pipe.  See if you can work out what it is made from! It is small enough to not be noticeable, but should be large enough to keep the rain entering the stove and causing damage.

    Now finished replacing brake pads, I assisted Matt with fitted the cowl to the chimney. The stove pipe was drilled and tapped in 3 locations to accept M10 bolts, which also will help to prevent the inner flue tube from wobbling inside the outer sleeve. Matt then painted the stove pipe, and the 2 torpedo vents in black bitumen paint.

    Whilst these were going on, Jake had painted the East side step irons in black bitumen once the old step board had been removed. Jake then primed the new step board once a chamfer had been planned on to the edge. Matt got his signwriing paint out and picked out the lettering on the handbrake standard.

    The day finished with Nick and I cutting out some filling pieces for some external pockets and priming them. Matt has also sign written our sign. 

    Sunday rolls around, and Matt is off playing with a Phantom. 

    Nick, Jake and I fitted the east side stepboard, with was still slightly tacky. Once fitted we found some of the step irons were not vertical.  We used a 5 ton ratchet strap and various landscape features to pull the irons back to vertical. Once we’d done this, we drilled the board and bolted it into position.

    We then let Jake loose with the bitumen paint again to paint the stepboard. Jake left Nick and I at 1400 to entertain visiting family. Nick and I journeyed to Swithland to retrieve components stored in the van train to begin our next project! Read next week to find out what this exciting new project is!